dtashmore547
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- Joined
- Jan 8, 2020
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hi @mper just updating my problem hopefully for anyone else having similar problems. after testing on Ispindel software and getting similar results and also the same on the gravitymon software and a esp32c3 build with the same issue I found I had to place the mpu6950 completely horizontal on all planes to get the correct calibration and 0 to 90 degrees of movement, I hadn't realized this when setting up initially and just had it level in the container which had the chip resting at an angle off horizontal. all is correct now thanks.