So, I have this Barley crusher that has crushed about 60 pounds of malt in its lifetime. Last night after milling my grain bill for my brew today, I noticed it didnt seem quiet as fine as it has in the past... not bad, but not the same.
So I check the gap... somehow it was opened up to about 1.038 from about 1.035.
Wow! At "1.035"" you can pass pin ball machine balls thru your mill, I couldn't let this one pass Pol.
I must ask what type of surface is the set screw contacting?
Flat surface with a flat surface at the end of the set screw or
is there a machined radius on the adjusting knob with a radiused
end of the set screw to match and contact against?
The MM-3 has a machined 0.0625" radius in the adjusting knob with a hand sanded
radius (looks like off a 1" wide belt sander) added to the thumb set screw to form a radiused end. The different radius plus not round on the thumb set screw caused the adjusting knobs to rotate when tightened down blowing the set gap all to hell. One egg shaped radius thumb screw had a radius larger than on the adjusting knob the other smaller which was less of a problem rotating the knob. The larger radius of the set screw as well not round would make the adjusting knob rotate when tightened every time no matter if swaped to the other end frame. I found that adding a piece of 0.250" brass stock machined with a 0.0625" radius end made on the lathe and
5/16" long with the other end flat only with a sight chamfer on the edge. The thumb set screws polished with a even and round radius that now contacts and rotates on these brass slugs with a small dab of grease preventing this rotating problem of the adjusting knob when tightened down and locking the set clearance.
On your BC if the adjusting knob to set screw are just two flat contact areas the use a brass slug with a flat at both ends. I still have 0.4375" (7/16") of thread for the locking thumb screw, plenty of threads to not worry about stripping out the aluminum threads.
I find the soft brass bites the hard stainless surface better than the stainless and steel thumb screw contact hence no pliers for extra tightening as per MM instructions besides I solved the set screw rotating the adjusting knob at the tightening set point. A lot less finger and thumb pressure is required on the locking thumb screw with the knob locked tight not rotating or slipping out of adjustment.
Maybe this fix I did to the MM-3 will apply to the BC mills also, your call.
This allowed for quick one shot adjustments or gap changes taking less than a minute
to reset both sides and recheck the new settings.
Sorry for the Novel, needed to reply here.