Coldbreak Brewing HERMS Giveaway!

HomeBrewSupply AMCYL Brew Kettle Giveaway!


Home Brew Forums > Home Brewing Beer > Electric Brewing > Soldering a 1" Lock Nut to Sanke Keg, with Pictures
Reply
 
Thread Tools
Old 05-03-2011, 10:39 PM   #41
hammis
HBT_SUPPORTER.png
Feedback Score: 0 reviews
 
hammis's Avatar
Recipes 
 
Join Date: Mar 2010
Location: canada
Posts: 305
Liked 5 Times on 5 Posts
Likes Given: 3

Default

nicely done quaffer!


hammis is offline
 
Reply With Quote
Old 05-03-2011, 11:55 PM   #42
pickles
HBT_SUPPORTER.png
Feedback Score: 0 reviews
 
pickles's Avatar
Recipes 
 
Join Date: Feb 2008
Location: Columbus
Posts: 2,019
Liked 49 Times on 41 Posts
Likes Given: 23

Default

Quote:
Originally Posted by Bobby_M View Post
The only difference between soldering and brazing as far as I know is temperature required. The filler material always has a lower melting point than the two materials being joined.
I soldered the fittings on my kettles with great success. I noticed though that I torqued on one too much and it cracked the solder, then leaked a bit. I just resoldered. However, I brazed a few tri-clover fittings to some 1/2 ss tube and can tell you that its MUCH harder than the solder. The joint got cherry red and the flux kinda twinkle a bit and it looked like some fusion was going on. Now I know it wasn't "welded" together, but i was able to grind the joint smooth and there is no visible seperation between the two pieces.


__________________
Gaptooth Brewhouse
pickles is offline
 
Reply With Quote
Old 01-15-2012, 07:31 PM   #43
runningweird
HBT_SUPPORTER.png
Feedback Score: 1 reviews
 
runningweird's Avatar
Recipes 
 
Join Date: Dec 2009
Location: State Line, PA, Pennsylvania
Posts: 2,109
Liked 87 Times on 63 Posts
Likes Given: 47

Default

I just came across this post and it really makes me want to try it on a keggle brew kettle. What did you use to keep the element contacts dry? a box?
__________________
My 6 Tap Long Draw Tower Build:
http://www.homebrewtalk.com/f35/long...-tower-271578/
runningweird is offline
 
Reply With Quote
Old 01-15-2012, 08:19 PM   #44
TheDom
Feedback Score: 0 reviews
 
TheDom's Avatar
Recipes 
 
Join Date: Oct 2007
Location: Fort Myers, FL
Posts: 382
Liked 4 Times on 4 Posts
Likes Given: 2

Default

I think I remember seeing someone basically cutting a hexagon out of the back of a box and soldering it to the side of the kettle around the nut. I'll be doing that to my BK here in the next few days.
TheDom is offline
 
Reply With Quote
Old 01-31-2012, 03:17 AM   #45
homebrewdude76
Feedback Score: 0 reviews
Recipes 
 
Join Date: Jan 2012
Location: Chesterton, IN
Posts: 161
Liked 2 Times on 2 Posts

Default

When you solder the hex nut on the keg you are not able to dimple it - correct?

If you were to dimple it, is there something that can be soldered on and still be flush enough for the element? Anyone tried this?
homebrewdude76 is offline
 
Reply With Quote
Old 01-31-2012, 03:46 AM   #46
epcgordy
Feedback Score: 0 reviews
Recipes 
 
Join Date: Sep 2010
Location: Seattle
Posts: 33
Liked 1 Times on 1 Posts

Default

On my kettle, I used the dimple method with a 1" half coupler soldered in. The half coupler provided a perfect surface for a silicone o-ring to seal. I used a weatherproof box, almost identical to Kal's installation to cover the connection. It works great, hasn't leaked a drop.
epcgordy is offline
 
Reply With Quote
Old 01-31-2012, 04:11 AM   #47
Bsquared
HBT_LIFETIMESUPPORTER.png
Feedback Score: 0 reviews
 
Bsquared's Avatar
Recipes 
 
Join Date: Oct 2006
Location: San Diego
Posts: 1,830
Liked 58 Times on 53 Posts
Likes Given: 22

Default

Quote:
Originally Posted by epcgordy View Post
On my kettle, I used the dimple method with a 1" half coupler soldered in. The half coupler provided a perfect surface for a silicone o-ring to seal. I used a weatherproof box, almost identical to Kal's installation to cover the connection. It works great, hasn't leaked a drop.
What size hole did you drill for this. I did the OP's method for my HLT because the 1-1/2 hole I drilled for the coupling was too big so I brazed on a 1" lock nut. I still need to put an element in the kettle and I'd like to do the dimple and braze a half coupling on.
Bsquared is offline
 
Reply With Quote
Old 01-31-2012, 04:31 AM   #48
epcgordy
Feedback Score: 0 reviews
Recipes 
 
Join Date: Sep 2010
Location: Seattle
Posts: 33
Liked 1 Times on 1 Posts

Default

IIRC, it was a 1 1/4" hole for the half coupler using the dimple tool. No need to braze, with the dimple and solder you can get a very strong joint. Check the Soldering Stainless Steel thread in the DIY section. There's a tremendous amount of info in there.
epcgordy is offline
 
Reply With Quote
Old 01-31-2012, 07:28 PM   #49
Bobby_M
Vendor and Brewer
HBT_SPONSOR.png
Vendor Ads 
Feedback Score: 4 reviews
 
Bobby_M's Avatar
Recipes 
 
Join Date: Aug 2006
Location: Whitehouse Station, NJ
Posts: 22,751
Liked 1300 Times on 854 Posts
Likes Given: 35

Default

In trying to decide between a flared opening with 1" half coupling and directly soldering a locknut, I think the nut wins. For one thing, the threads are both NPS and there is no question that the gaskets will mate before the threads interfere. Then next reason is that there is more surface area for solder to bond to. Last, no flaring tool needed.


__________________
Welcome to BrewHardware.com. I love you.
New 100% Stainless Steel Heating Elements are IN! ULWD 5500w Ripple, 2000w, 1500w, etc
Chugger Pumps, Pump Kits, Camlocks, Sightglasses, Clear USA made Silicone Tubing, RIMS, Electric Install Parts, etc.
Bobby_M is offline
 
Reply With Quote
Reply


Thread Tools


Similar Threads
Thread Thread Starter Forum Replies Last Post
Using 1" Camlock for quick release element? SenorWanderer Electric Brewing 31 12-02-2011 02:54 PM
Question about my dryer outlet and a 3500watt element (w pictures) rtt121 Electric Brewing 24 11-10-2010 07:41 PM
Electrical Soldering setups, what do you have/what do you recommend Boerderij_Kabouter Electric Brewing 20 11-03-2010 06:43 PM


Forum Jump

Newest Threads

LATEST SPONSOR DEALS